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Spitfiredriver71

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Posts posted by Spitfiredriver71

  1. It's an MS3. 

    I am also playing around with a Bosch knock sensor.  I have made a circuit to filter the low frequencies out and just need to fine tune the gain. Then I can advance the timing a bit without having to worry. 

  2. I tried connecting the rocker cover to the air filter side of the throttle body today and after 15 minutes  not a drop of oil. The port on the throttle body looks like it acts like a venturi so seems to work for my needs. 

    The piping was just what I had lying around to do the test so will need sorting but I have attached a photo. 

    I tried to make the manifold look similar to a TR6 plenum.

    IMAG1163.jpg

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  3. Hello Clive

    I did some testing  again today and with the breather filter removed, the oil stopped coming  out.  As soon as I put it back on, oil came out the dipstick.

    I can blow straight  through  the filter and it offers next to no restriction but without it connected it does not leak. 

    I was thinking the same thing earlier about connecting it to the throttle body. There should be a slight vacuum as the main air filter will cause some restriction. As it would be on the outside of the butterfly  it should  not affect the vacuum reading  to the ecu.

    I will try the leakdown test on another  engine when I get the chance. It may be that my tester is rubbish.

    The bores were honed when I rebuilt it.  It was a replacement engine so I stripped it as a precaution and as everything was in spec I just replaced bearings and piston rings. 

     

  4.  Clive

    I was trying  to avoid connecting it to the manifold  as I think it will upset the vacuum. It used to cause problems  with the carbs which is why  I fitted the lambda sensor in the first place.  With it connected  on overrun the car would stall (really  lean)   With it vented it worked fine. 

    Ian

    It was at 40psi. The instructions said to set the compressor to between  40 and 60psi.

    I will try warming it up this afternoon  and trying again at a higher  pressure.

    It's certainly not a high quality  tester but I was hoping to find a definite problem.  It was just about in the green on the gauge  but I thought  it should  be higher considering the mileage since the rebuild. 

  5. I will try removing  the filter this afternoon. Has anyone done a leakdown test? 

    I did have a catch tank on a previous  setup but it still had a filter on the output.

    This is an ongoing  issue over many years. I might be trying to achieve the impossible with a triumph  that does not mark it's territory.

    Since the fuel injection I drive it a lot more and the oil everywhere I park is getting really annoying.

  6. It is a mark Iv but is a long way from standard. The rocker cover is the aftermarket  aluminum  Style and I just have a filter on the breather.

    The car is running fuel injection and fueling is good. It used to have hs4 carbs that sucked the excess crank case gasses but has always  leaked oil. 

    I built the bottom end 7 years ago and I wonder if I got the ring gaps wrong as it has excellent  compression, starts first time and does not burn oil.  It just seems to push it out. 

    If it take the filler cap off the oil leaks stop and it will sit on the drive running for 30 minutes without  losing a drop. 

     

     

     

     

     

     

  7. I have an oil leak from my spitfires dipstick.

    The car does not do many miles each year and has done less than 10,000 miles on the current pistons and rings but I seem to have excessive blow by. 

    On a standard compression tester I get good  readings on all 4 so was advised to try a leak down test instead. 

    I am getting 30-40% leakdown. I assume  this will be a ring problem as the air is coming out of the dipstick but wondered what numbers are realistic for an old triumph. 

    Modern engines achieve 10-15% but I assume they run tighter tolerances. 

    There are no marks in the cylinder walls  and there is no measurable step at the top.

    The car runs and drives well apart from its incontinece.

    Any ideas? 

    Alan. 

  8. Does anybody know what the clearances are for the main and bigend bearings for a Spitfire IV 1300?

    While I have the engine out I thought I would check the bearing tolerances with some plasti gauges.

  9. I have managed to get a new mainshaft for my 3 rail spitfire gearbox with the correct drive for my J type overdrive, but the clip from the old shaft looks very small on the new one as the gap is much larger. The clip is in between the 2 shafts in the photo. On the darker broken one it fits the gap after the splines but the machined area on the new one is much bigger. What does the clip do and is it needed? I have not found it in any catalogue yet.

    Clip.jpg

  10. Does anybody know if you can buy just the front part of the floor pans for a triumph spitfire in the UK.

    There are multiple options in the US but have only seen complete floor panels over here.

    I have the seats out and from the support back it solid but the front part has had water trapped under the carpet at some point and is a bit thin in places.

    Alan

  11. After cracking the mainshaft on my gearbox a few weeks ago I have been trying to sort out what is good and what needs replacing.

    The photo below shows the 2 sets of gears I have, however It has been a game of spot the difference. One has a thrust washer that locates on a ball bearing and the bush for 2nd gear and thrust washer for 3rd gear are one part. Does that mean the end float should be the same on both? Also there is a lot more movement on the synchro hub on the right, you can see the gap in the photo but 2nd gear seems to line up although it is wider.

    The only person that can supply the shaft seems to be Mike Papworth but I do not know which thrust washer I will need to use, ball bearing or not?

    Another question is which synchro hub should I use? the one on the right has rounded off edges in the first gear direction but the one on the left has a damaged tooth.

    Any advice gratefully received.

    Alan

    gear set.jpg

  12. Hello Peter

    I am in Basingstoke, Hampshire.

    I got the input shaft out by making a tool to press it out from the inside. The next problem is the bearing on the main shaft. I got it to move about 2mm by hitting the shaft with a large rubber mallet but 1st gear is now up against the gearbox casing. I assume the Haynes manual is talking rubbish about hitting the shaft though. I can not see how the gears can move up the shaft without taking the circlip off 3rd gear first. Feeling like a bit of an idiot over this. 3 days and only slightly further. I built the last engine and fitted it back in the car in less time than this.

  13. I tried a new bush and it made no difference to 3rd and 4th. With the gear box removed and the top cover off I can apply force to the 1st or 2nd synchro and get them to start to engage. The synchro hub for 3rd and 4th does not move at all. I looked in a spare non overdrive gear box I have and the hub moves fine in that box so the problem is definitely the 3rd and 4th synchro hub.

    How do I remove the constant pinion shaft?  Also will I be able to get the synchro hub off without removing the main shaft as I only have a problem with one bit?

  14. I took the remote selector off tonight and there was a black sticky mess at this joint. Not sure what it is called. Is there supposed to be a rubber or nylon bush here as the hole is huge? There is a small metal bush that I am holding in the photo but it is tiny compared to the hole below it. 

    Selector.jpg

  15. Hello Pete

    It is a 3 rail gearbox with J type overdrive. I did not check the oil but the overdrive normally drops out when the fluid is a bit on the low side so I have assumed there was plenty in there.

    The clutch seems to be disengaging fine as i can select any gear with the engine running and the car is stationary. When I had a weeping slave cylinder in the past reverse and first were difficult to engage but they seem fine at the moment.

  16. I was driving my Spitfire yesterday when half way home I had a problem changing from 2nd to 3rd, the gears grinded as if i had not used the clutch. The same then happened from 3rd to 4th.

    I stopped at the side of the road and can select all gears stationary with no problem and 1st 2nd work fine when moving. There is no strange sounds coming from the gearbox and once in gear it drives fine with no movement from the gear stick. I had the cir clip go that effects 3rd gear about 10 years ago so know it is not the same. When that happened the gear stick would move forward and backward with throttle input.

    I tried 3rd and 4th at a slow roll less than 10 miles an hour and goes in fine it just does not want to go smoothly at higher speed. I assume the syncro has failed but both 3rd and 4th within a couple of seconds and no noticeable wear before that moment seems unlikely.

    The ball and spring below the selector are fine as that was my first check. I guess it is going to be a gearbox out job.

    Any ideas? I have not worked on the gearbox for a long time so could be a steep learning curve.

    Alan

  17. I have done some tests on the part of the tank I cut out. The bottom is no de greaser. Top left is metal prep but not rinsed and top right is applied at 27 degrees C. Looks like it should not be applied on a hot day. I also tried a sample with spraying it with water and nothing made a difference apart from being too warm.  

    IMAG0468.jpg

  18. The surface temperature was that high in the sun to make sure it was completely dry. I believe it was 25 degrees yesterday afternoon when I used the sealer. The tank was in the shade at the time so 25 ish.  The bubbles started to appear about 30 minutes after draining. They then developed into blisters.

    Feeling very disappointed as I have spent a lot of time making the adapters and welding. I bought the TIG welder for this particular job and it has all been ruined by the tank sealer. I hope that POR will tell me what the batch code means. 341609. I bet it is old stock. Many hundreds of pounds and weeks of work down the drain.

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