Search the Community
Showing results for tags '1147'.
Morning all! My first post on the forum!! I am looking for an FC prefix 1147cc engine for a Mk2 Spitfire, can anyone point me in the direction of where I might find one? (GA/GD prefix would also work) I am based in Guildford, but happy to drive all over, I once drove to Blackburn for some other bits... Any help would be greatly appreciated! Cheers, Henry
Hi all I have just gone to replace the thermostat on the 1147 1965 Herald, firstly I found there isn't one fitted, so, fitted one to very quickly find out why there wasn't one fitted!! I now understand that the early 1200's didn't have a temperature gauge installed so this one has had a modified thermostat housing installed with a temp sender unit in the top, trouble is, the gauge intrudes so much that the housing wont go back on with a thermostat in there! Anybody had a similar issue? I'm wondering if there is anywhere I can get a shorter gauge to fit or alternatively, if I install a standard housing, would I have to install a later water pump housing to get a gauge on or is there any other way? As always, many thanks in advance for any advise. Regards Gary
Hi guys A few tips if you don't mind as I'm sure some of you must have had the issue! LITTLE BIT OF BACKGROUND: 1147 Herald which I got back on the road 500 miles ago has been running perfectly as I have gradually increased the distances, speeds and time of trips. slightly longer trip last week on the M way so higher speeds than normal and a longer trip, all went well, nice smooth running. ISSUE: Once off the motorway,car started stalling when pulling up so no tick-over every time I pulled up. After a couple of roadside stops and some tinkering with the volume adjuster and tick-over screw, all was back to normal and the trip back was as smooth as the one out. I have taken the car out this week and instantly, the tick-over issue has returned and the car running generally rough. ACTIONS SO FAR Checked compression's, all good Re-adjusted the tick-over and volume adjusters Replaced soiled fuel filter Replaced (very soiled) air filter (which also smelt very fuel rich) Adjusted timing which appeared to be slightly out Removed & cleaned carb mixture jet Checked points gap Checked plugs gaps (rich deposits on plugs) CURRENT SITUATION: Tick-over now good when warmed up and choke pushed full in ISSUE: Car is now very under-powered compared to previously, particularly at the higher speed end, 50mph, doesn't want to go any higher with foot flat to the floor and it was slow getting to that point. OBSERVATIONS: Some back-firing and carb popping when accelerating and slowing Temperature good and stead Oil pressure good Vacuum same as previously was NEXT STEPS: Any thoughts welcome guys and gals but do you think I'm right to be looking at: Carburettor Fuel delivery Re-looking at the timing Like I say, any assistance, thoughts, ideas very much welcome. All the best Gary