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Pete Lewis

TSSC AO
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Posts posted by Pete Lewis

  1. I have a long time ago with a 1300fwd that dropped a thrust and the crank machined the thrust locating lugs off the brg cap

    we had the crank ground and welded two new lumps on the cap to re support the thrusts 

    this lasted over 10 years of use 

    Pete

     

    • Like 1
  2. Will,  chasing your tail is all part of the "fun" 

    classics can and do run really well ,as good as when they  were new  but getting there can be a 

    long slow route of unravelling previous concoctions  of poor meddling .

    it can take a season to get to know your car and its traits 

    you will get straight answers on this forum , never follow daft ideas from the pub of FB 

    unless you want to chase myths !!!

    have fun   it will all come together 

    Pete

    • Like 1
  3. we made some simple wooden spars with a slot in each end to slot over the seal flange to make sure the door gap 

    did not close up on tightening the rear tub 

    i recommend a pair of solid mounts on the diff cross member  

    you dont want the tubs to shift  at the first speed hump which with rubbers all round has no positive fixing

    do have a think about a good wire earth bond between all sections while it in bits 

    saves a lot of volt drop on tail lamps etc .

    Pete

     

  4. well spark plugs are the life and soul  but sooted can lead to plug failure 

    here is a link to some thoughts on modern plugs dont suit carb /choke operation as well as they used to

    once the ceramic is "contaminated" by poor fueling you seem its not cleanable lots of alternatives but 

    the lack of glaze does seem to plague us , less choke /drive it quick is the best solution 

    any back fires point to a dodgy condenser ( but if electronics are installed you wont have one) 

     

    • Like 1
  5. i dont think your running headache is anything to do with the base engine its all to do with ancillaries 

    R is resistive theres a good few you tube examples testing the reduction in HT 

    fine on a 35kv modern but not good in our lower 22kv HT 

    so its been clear to me that missfires are caused by corking up the HT    some use them and have no problem 

    so its stick to simples not go chasing red herrings 

    blocking the intake vents can cause chaos

    there are some awful dizzy condensers about  best get one from distributor doctor 

    Reconditioned Lucas distributors, rebuilt Lucas distributors, recurved Lucas distributors from Distributor Doctor

    does delco parts too   have a read about rotor and condensers 

    Pete

    • Like 1
  6. as a 1500 is it still on waxstat jets ????  a known nightmare

    as you have been messing with the carbs have you disturbed the fuel hoses   as refitting will make rubber slivers 

    these can block jam up the float needle valve .

    there is an easy fix to waxstats  will use 2 x 2  1p pieces .

    dont use plugs with an R in the suffix.

    soot after choke will take a Loooong time to burn off the plugs .

    what air filters do you have ., makes sure the filters gaskets are not obstructing the carb vents .

    more to follow as you give us more clues 

    Pete

     

  7. If you have a current insurance with P james then you are automaticaly cover to drive other members?  cars 

    and I promote having an MOT every year as this proves out the brake balance which you cant DIY 

    and might find the one thing you felt was fine when it had degraded to a concern 

    good for peace of mind and safety to others 

    Pete

     

    • Like 3
  8. the very front two are just one metal no rubber here .

    these two in the front rigger are location and have little adjustment one rubber on all others with as many spacers as needed to align 50 yr wonky body with 50yr wonky body

    when refitting the body its well worth earth bonding all body and chassis sections with a decent earth wire ,front to back .

    does  save a lot of voltage loss to the bonnet and tail lamps

    Pete

  9. or an 8x4   4 axle  and 80 nuts      

    had a torque meter for checking production... looked   more like a parking meter up to 600 lbft   yes took some wielding 

    always gave the audit task to the strongest  ,   anyone weedy couldnt hack it 

    Pete

    • Like 1
  10. that gasket has let go due to lost clamping ....soft washers and lost torque

    its the nuts that will be black not the studs   ( sorry i left 'nuts' out )

    Pete

  11. as a infrequent  i just stuff the hole with paper towel or similar   to keep it from attracting debris

    no reason why you just remove the remote hsg,  then smaller hole exposed   but a bit less clearance 

    removing the remote /top cover just aids clearance and the angle of dangle to clear the bulkhead opening 

    no real need to get carried away 

    Pete

    • Thanks 1
  12. well at least the carbs are CDS  simple  no frills   with cold satrt choke on the front unit   tubed to the rear one  thats good 

    better studs   unlikely that that is possible , its the nuts and washers are the weak link here  not the studs  

    the 42-46lbft is quite adequate for the 3/8 studs    the washers deforming is the main snag  and never use std 3/8 nuts they wont take more than 31lbft  

    the orig Nuts are  oil quenched  black finish  .  mini flanged nuts are the way to  progress but bear in ming knurled washer faces can absorb tightening torque

    Pete

     

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