Pete Lewis Posted May 10, 2018 Report Posted May 10, 2018 more used to answering than asking but hey ho here we go this 1500 spit had bugged me for some time with its erratic unhelpful back fires /spits/ misfires and the ocsional good running waxstats off , and fitted fixed jets ,these proved hopeless and 2p repair to the waxstats refitted them, it has new point + added an old classic condenser, tappets ok , fuel clear and well supplied,, filters std. fitted right way up .carbs are fine but need far more richness than std pre run settings these are ball bearing topped HS4 . correct needles , i dont expect a 421 to need much needle revisions , with std filters . compressions all 4 are 110 lbs, these are all even but below the expected 130+ deterioration since some guy fitted the 421 manifold, the gasket looks ok and all fixing are in place so air leak is possible ,not done a squirt test over the joint yet even calibrated the compression gauge and its spot on not check cam timing but this is all neat tidy everything is as should but runs like a pig then found no rear brakes and a failed PDWA valve so no fluid now and a coolant bypass tube sealed with filler , the list grows but the running is hopeless not my normal scene , im supposed to fix them not grow warts . any out the box thoughts ??? Pete
Anglefire Posted May 10, 2018 Report Posted May 10, 2018 Points gap was what was wrong with mine when it ran crap after its transplant. Other than that I would be guessing as I'm clearly no expert!
dougbgt6 Posted May 10, 2018 Report Posted May 10, 2018 Pete, Occasional good running then dodgy running sounds like something in the timing system is slipping, moving, popping back? How's the timing chain and/or cogs? You haven't mentioned the dizzy? How is it? Have you checked the flux capacitors? Doug
Pete Lewis Posted May 10, 2018 Author Report Posted May 10, 2018 Will be getting the car back to rebuild the brakes, amd more gremlins will appear on that job, bet the Mcyl needs a rebuild also Points are new , timing is on the mark , but not checked the cam timing Just dreaming the firing back out the carbs is internal crossover And as for flux yes I am ..fluxed out Pete
dougbgt6 Posted May 10, 2018 Report Posted May 10, 2018 Prevarication! What about the dizzy?!! Flux capacitors are only on Delorian's and Star Trek, obviously. db
Nick Jones Posted May 10, 2018 Report Posted May 10, 2018 Low compressions (if the gauge used is known to produce normal readings on other engines) and generally poor running suggest the following checks are needed valve clearances (tight tappets due to seat recession) Valve lift (worn followers/lobes) Valve timing. Nick
Clive Posted May 10, 2018 Report Posted May 10, 2018 Cookies GT6 did the backfiring out the carbs etc a few years ago at SEM, and that was cam timing sprockets jumped many teeth (turned out teeth had more or less gone) Unusual, we were all scratching our heads at the time, and I remember saying how unlikely it would be if the timing had moved that much Wrong again...
Pete Lewis Posted May 10, 2018 Author Report Posted May 10, 2018 Doug dizzy is as new points new did fit an old condenser no change Nick /Clive cam timing is on the agenda , tappets are fine but at times its quite good.. it not fuel or blockages in the supply , certainly no rubber slivers something very odd about whats going on ..maybe me seaweed has dried out in the sunshine ??? its set rich which stops the fire backs out the carbs the head has unleaded exhaust seats fitted have calibrated the gauge up to 8 bar ( 120 ish )and its spot on, couldnt go any higher as the fitting wanted to part Pete
Nick Jones Posted May 10, 2018 Report Posted May 10, 2018 Manifold gasket making marginal contact - sometimes air leaks, sometimes not? 120 psi is a bit low though..... is it known what the cam is? Nick
dougbgt6 Posted May 11, 2018 Report Posted May 11, 2018 13 hours ago, clive said: Cookies GT6 did the backfiring out the carbs etc a few years ago at SEM That's what I was thinking about, although I'm sure he told me it was IOW, not that it matters. Doug
Pete Lewis Posted May 11, 2018 Author Report Posted May 11, 2018 Nick no idea what cam , i expect std, but thats a guess two things we got worn out and not given up but a days work going nowhere got the better of us (thats Ray ad I) it did run better on the conversion jets although no matter what you realigned the choke would not return hence back to the 2p repair , jet heights all measured and equal . whay with all the messing about changing the jets , finding no brakes and more time ran out and the ideas about a squirt over the gasket and a cam time check were pencilled in but never concluded , tea and cake was a stronger calling she did drive home without any pops or bangs but obviously too rich as i set the jets down to get some running when the car returns will do the two oustanding ideas return the needles to a proper setting and then find a box of matches as a side the pdwa valve kit from Rb is £19 and £6.70 from BCS ebay they say its only for stag,, bit odd as that girling valve and repair kit 155071 was fitted to a whole plethera of makes the suns shining and we have 35 off to. McAplines Steam trust at Fawley Hill tomorow we will see Hmmmm !!!!! pete
dave.vitesse Posted May 11, 2018 Report Posted May 11, 2018 Pete, I guess you have tried the roto arm, dizzy cap and sticking carb piston. The problems you have found changing over to standard jets where they stick when returning the choke is a problem with these repro jets. Changing the angle of the wire link holding the jet in position can help. Though the main cause is likely to be drag on the jet by the fuel pipe. Whatever it's a pain. Dave
Pete Lewis Posted May 11, 2018 Author Report Posted May 11, 2018 hi dave its got a dizzy doc rotor and cap , dont expect lead as this is to variable, if it was just one cyl missing you could find the culprit the choke rod was bent /shouted at /cursed /and stared at / it was just useless tried shortening the bowl feed a few mm to unload the pressure of the ups and downs ... the kits take some ingenious trial to get the operting all as should but being a meccano fan it soon sorted which spring went where on what lever. an expensive mistake its got a giant case of rubber slivers and worse ..........but without them !!!! Pete 1
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